PECM Issue 30 2018 | Page 82

THE AEMT ENSURES ENERGY EFFICIENCY IS MAINTAINED DURING SERVICE AND REPAIR n extensive joint research project conducted at the University of Nottingham found that energy efficient motors remained within plus or minus 0.5% of their original efficiency after being repaired by a good service centre. This is within the specification tolerances of the label and efficiency banding. These tests were backed by a number of leading international industrial organisations and Government Departments in the UK and USA. Tim Marks of the Association of Electrical and Mechanical Trades (AEMT) reviews the projects and their findings. A Sometime ago, members of the AEMT and the American Association EASA worked together to establish "The Good Practice Guide to Maintain Motor Efficiency" after repair. The Good Practice Guide has since been used by members of the AEMT and EASA internationally to ensure that any repairs carried out retain their rated efficiency. The Good Practice Guide and research details are freely available from the AEMT Website. The first Best Practice Guide to maintain Energy Efficiency was produced by the 82 PECM Issue 30 AEMT in conjunction with Department of the Environment, Best Practice Programme on Energy Efficiency. It was led by Professor David Walters, who had previously led the Brook Crompton design team on their ground breaking W range of energy efficient motors. The project remains the largest study of its kind with tests being carried out on 34 electric motors. These were 5.5 kW D132S machines supplied by manufacturers. They included 13 old design aluminium motors, 13 original design "Energy Efficient" motors, and 8 "higher efficiency" motors. A major difference between the machines was the quality of their stator laminations. The "Higher Energy Efficient" machines were some of the first to use a high grade steel coated with an inorga nic based L3 film. This heat resistant varnish film increased the ability of motors to withstand annealing temperatures, and withstand multiple burn out temperatures without any detriment to the core laminations, as shown by tests during the project. Improvements in the electrical steels using L3 or better have formed the basis of new energy efficient machines over the past 20 years. This is shown in figure 1 extracted from the original project. A few years later the original research programme was expanded to include larger machines up to 225 kW. Several Government Departments, electro- technical companies and industry groups - both domestic and international - were approached to join a wide-ranging project to broaden the base of the next research project. Sufficient machines were included to give statistically reliable results, which increased the cost of the exercise. To mitigate this, the AEMT invited representatives of the US Department of Energy and through them the US repair trade association (EASA), both of whom agreed to join the project. The AEMT then approached their own national government for support and further sponsors were encouraged to join. The final list of participating organisations was impressive, and included the UK Energy Efficient Best Practice Program, UK Ministry of Defence (Navy), UK Water Industry Research Centre, and British Nuclear Fuels. Ten motor manufacturers also became partners to the project providing motors, technical data, and assistance for the study. These included ABB, Siemens,